A dynamic and engaging banner for USLIVE.com, featuring bold typography and vibrant visuals that represent the latest in breaking news, entertainment, celebrity updates, lifestyle trends, and current events. Designed to keep readers informed 24/7 with the most relevant and up-to-date stories.

Maintenance and pilot failure are cited in report on fatal 2022 New Hampshire plane crash

KEENE, N.H. (AP) — Improper maintenance and the pilot’s failure to abort takeoff likely caused a small plane to crash into a building in New Hampshire in 2022, killing both people on board and sparking a fire, the National Transportation Safety Board said in its final report.
The single-engine Beechcraft Sierra crashed into a two-story barn connected to a multifamily apartment building north of the Keene Dillant-Hopkins Airport the night of Oct. 21, 2022. All eight people evacuated the building and were not injured.
Killed in the crash shortly after takeoff were Lawrence Marchiony, 41, of Baldwinville, Massachusetts, and Marvin David Dezendorf, 60, of Townshend, Vermont.
The plane had last flown about 14 months earlier with both men in the cockpit. They had experienced “poor takeoff and climb performance during a flight,” the NTSB said in its report, dated May 30.
In the 2022 flight, witnesses reported that as the plane accelerated on the runway, “the engine did not sound normal” and the “poor” sound continued once it was airborne.
An examination of the plane showed improper maintenance of the fuel injector nozzles, the NTSB said. The nozzles were missing inserts or restrictors and showed extensive leakage, the report said.
A mechanic had reported that the nozzles had been cleaned as part of the plane’s annual inspection.
“It is likely that at some point after removing the inserts or restrictors for cleaning, they were not reinstalled,” the report said.
Contributing to the crash was a mechanic’s decision to return the airplane to service with the engine unable to attain its full power, the report said. An analysis indicated that as the plane became airborne and immediately before impact, the engine was operating at about 11% less than maximum power and likely significantly less at the start of takeoff, the NTSB said.
The agency said the mechanic “likely incorrectly identified” the maximum power during a post-maintenance engine run.
Marchiony and Dezendorf likely did not recognize that the engine wasn’t at full power as the plane was accelerating. But both “should have recognized that the ground run was excessive and aborted the takeoff while still on the runway,” the report said.

A dynamic and engaging banner for USLIVE.com, featuring bold typography and vibrant visuals that represent the latest in breaking news, entertainment, celebrity updates, lifestyle trends, and current events. Designed to keep readers informed 24/7 with the most relevant and up-to-date stories.
TOP HEADLINES

Trump Enacts Tariffs on Canada, Mexico

The imposition of tariffs by U.S. President Donald Trump on Canada and Mexico came...

LeBron James Eyes 50,000 NBA Points Milestone

Another Remarkable Achievement Awaits LeBron James: Approaching the 50,000 NBA Points Mark. LeBron James...

Militants Attack Military Base in NW Pakistan

Bannu, a city in northwest Pakistan, experienced a dramatic attack on Tuesday when twin...

New Orleans Mardi Gras Festivity Thrives Amid Weather Worries

As dawn broke over New Orleans' historic Treme neighborhood, a crowd adorned in skeleton...

Arab Leaders Convene in Egypt Over Alternative to Trump’s...

Arab leaders are convening in Cairo to advocate for an alternative approach to the...

Vance: Minerals deal curbs Putin more than foreign troops

WASHINGTON — Amid ongoing discussions about how to prevent Russian aggression in Ukraine, Vice...